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OverviewDuring a flight test study of the noise effects on laminar flow on the outside surface of a simulated engine nacelle, an intense acoustic response was observed. The aircraft speed at which this signal occurred and the frequency content of the signal fell within the test conditions of the experiment and had to be eliminated prior to continuing. The signal was identified as an aerodynamic excitation of an acoustic mode in the simulated by-pass duct of the nacelle. By modifying the trailing edges of the support struts of the nacelle, the aerodynamic excitation was changed enough to eliminate the resonant response of the offending duct modes, eliminating the unwanted acoustic problem. Schoenster, James A. Langley Research Center NASA-TM-102585, NAS 1.15:102585 RTOP 506-80-31-06... Full Product DetailsAuthor: National Aeronaut Administration (Nasa)Publisher: Createspace Independent Publishing Platform Imprint: Createspace Independent Publishing Platform Dimensions: Width: 21.60cm , Height: 0.20cm , Length: 28.00cm Weight: 0.111kg ISBN: 9781725008779ISBN 10: 1725008777 Pages: 36 Publication Date: 09 August 2018 Audience: General/trade , General Format: Paperback Publisher's Status: Active Availability: Available To Order We have confirmation that this item is in stock with the supplier. It will be ordered in for you and dispatched immediately. Table of ContentsReviewsAuthor InformationTab Content 6Author Website:Countries AvailableAll regions |
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